SystemsGuy

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  • in reply to: Z-Axis Headaches! #3652
    SystemsGuy
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    So after a bit of a rest, and coffee, I’ve solved my problem, but I’m not 100% sure I understand why.  Setting the max_travel_velocity t0 < 1000 seems to work – which I assume is dropping the step rate the board is try to push out to the motor, and making things happy.

    Is this a function of my motor choice or simply the max the board can support – or both?!

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